I opened the bonnet of the 3rd gen the other morning to check coolant levels, and found in the overflow bottle what appeared to be brown, oily muck. Opened the cap on the rad to find the same thing.
In a panic I checked the indise of the oil cap and the dipstick, but thankfully all I found there was black oil.
I got a mechanic to look at it (not my usual guy), and he immediatly said that I had a cracked head, common to these 3 litre engines, and that it would basically be a replacement engine job.
The surf had been sitting idle for a couple of weeks while we were away, and the coolant was clear at that stage. After we came back I had only been doing short 2km or so runs before the coolant turned to sludge. It hadn't overheated, and it wasn't down on power or fuel consumption (my fuel consumption is improved by 20% at the moment after a dose of STP diesel treatment a couple of fills ago; I had been gettin 400km to the tank, and I'm currently getting 500. Might try diptane soon, as I've been hearing good things about it).
Because of that I hoped that it was only gunk coming to the top, so I got the coolant system drained. On Monday it was flushed about 4 times, and the same again today. It now has a proper antifreeze mix, and they did some kind of vapour test to try and detect if there was any oil getting into it this morning before they flushed it again, and that test came back clear.
Will sort out a compression test in the next few days for peace of mind.
Has anyone else gone through this?
In a panic I checked the indise of the oil cap and the dipstick, but thankfully all I found there was black oil.
I got a mechanic to look at it (not my usual guy), and he immediatly said that I had a cracked head, common to these 3 litre engines, and that it would basically be a replacement engine job.
The surf had been sitting idle for a couple of weeks while we were away, and the coolant was clear at that stage. After we came back I had only been doing short 2km or so runs before the coolant turned to sludge. It hadn't overheated, and it wasn't down on power or fuel consumption (my fuel consumption is improved by 20% at the moment after a dose of STP diesel treatment a couple of fills ago; I had been gettin 400km to the tank, and I'm currently getting 500. Might try diptane soon, as I've been hearing good things about it).
Because of that I hoped that it was only gunk coming to the top, so I got the coolant system drained. On Monday it was flushed about 4 times, and the same again today. It now has a proper antifreeze mix, and they did some kind of vapour test to try and detect if there was any oil getting into it this morning before they flushed it again, and that test came back clear.
Will sort out a compression test in the next few days for peace of mind.
Has anyone else gone through this?
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